Trial & Error

For a few years I have been doing some tweaks here and there on the car, one of those bigger projects was the LED bulbs all round. At the back of the car the rear licence plate bulb was the biggest pain to source one that would fit in the original factory housing. I tried many variations some were close others not so. The left pic below is the now dedicated draw now allocated for bulbs, the right pic shows the original bulb (copper bottom) in the middle, with the other trial and errors bulbs around it. Some were too long, too wide or the bulb glass (plastic) to bulbous to fit under the lamp holders glass cover itself. Then there was front focussed light, 360o light shine, light pattern, colour temperature, brightness, bottom housing fitting, wattage etc etc. Some bulbs what I thought would look good were in fact quite poor lighting options when plugged into my dummy rig to see what they would look like before I took the holder off the rear bumper and started making a mod to the wiring loom.

I spent many an hour making mods to a couple of the bulbs that had potential with the Dremel in a vain attempt to make them fit. A slight slip of the Dremel grinder ruined a promising bulb that was just a bit to wide, luckily those bulbs came in pairs.

The before and after of the grinding was fine, there was no cover for these LEDs themselves which shouldn’t be to much of a problem as the bulb sits behind a opaque glass bowl if you like. To make the bulb fit under the glass properly it would need more work on one side of the bulb fitting, in doing so it would be getting dangerously close to the LEDs themselves. Before I got carried away I quickly put it back together with the glass cover sort of half in place held by a bit of clear tape to see what it would look like at night, it wasn’t good. There was so much white light I could expect a pull over from the local plod in their donut cars as you’re not supposed to show white to the rear in the UK. This bulb was on another level and would be more like towing a WWII search light behind me.

That bulb was discarded and the original put back in for now. After many, many searches and I eventually found a match same size bulb and voltage. Best of all it was a comparable wattage to the original bulb, I placed the order which was shipped from China (of course) to the UK.

The new bulb was still quite bright, but I figured it should be OK.

This LED bulb thing is all a little bit of a moot point as I tend not to drive at night anyway. However, if I needed to, then the LED bulbs are a significant improvement for safety. The reason I mention all this now is because of a recent trip trip to Mustang Maniac where I watched as they were making a custom fit LED board for a customer’s car. They had to make bulbs from bulbs and then set the brightness. I wasn’t aware that it could be done to that degree and spent some time with Mark to see how I could make their ideas work for me.

I purchased a box of various resistors taking on board the advice I was given. This box is complete overkill of 350 pcs, I only wanted one or maybe two variations of a resistor. The complete box was the cost only a large coffee so I couldn’t complain.

There’s a lot to understand about resistors; basically wattage and resistance describe two different, but connected processes a resistor performs in a circuit. First is Ohms (Ω) tell you how much the resistor limits electrical current, a higher Ohm value means more resistance and less current flow. Second is Wattage (W) tells you how much power the resistor can safely dissipate as heat without burning out. So the Ohms value sets the electrical behaviour, while the Watt rating sets the physical durability. A resistor with the right resistance but too low a Wattage may overheat, whereas a resistor with the correct Wattage but wrong resistance will change how the circuit works. You can also fit a resistor either direction as they aren’t polarised. If you need a specific Ohm rating you can add one after the other to achieve the correct rating.

As the licence plate bulb only has a single live feed, the earth is handled via the bodywork. The live feed just needs an inline resistor so the LED’s bulb brightness is reduced as a result.

In the trunk the live is taken from the rear drive lights feed via a T-junction split and a connector. The wire then passes behind the rear bumper to the lamp holder out of direct line of sight. This will be a quick task to make up an insert male and female fitting at each end to connect it back up again. If I don’t want to use the resistor, I can just remove the inserted resistor and reconnect the original wire back to the normal live feed voltage.

When I rewired the car I didn’t use all the options of the American Autowire kit, that left me with various amounts wires of different colours and a number of connectors to go with them. A short clip from one of the coils of wire I used was the same gauge as the live feed about to be modified.

The short wire was cut in half and each end of the wire was tinned with the soldering iron. My American Autowire crimps were pulled out of retirement and used to secure the male spade connector and protected with heat shrink.

The resistor I chose was a 330 Ohms which should roughly half the output. In order to make the resistor lay flat inline; wrap the wire leg of the resistor around a small jewellers screwdriver the same size as the gauge of wire to be used forming a tight coil. I didn’t realise the picture was out of focus (sorry), but you get the idea. Trim the coil flush to make sure no sharp parts are sticking up and potentially cause a short.

Thread the new wire into the coil and add some flux, fresh solder on the iron and tap it onto the join you just created. Before the last female spade connector is added slide over the shrink wrap and then repeat the process and solder the other end of the resistor. Add a spade protector on the female spade connector and crimp. Once completed and fully heat shrunk, I checked the resistance with a multi-meter to make sure connections were solid and working.

To create the inline project that I wanted, the live feed wire needed to be modified to add the additional spade fitting rather than a direct solder of the resistor, my fail safe if you like. This additional could then be re-joined in seconds to the main loom if needed, or connect another resistor inline back to the main rear end wire harness. I remade the duel spade (T-junction) split along with the new single connection needed for the lamp holder.

With the new inline resistor in place it only added a couple of extra inches so the extra length could easily be hidden back behind the filler cap support. Here the fittings are in place to recreate the original look before I added the resistor.

With everything in place the garage door was closed and turned the lights off. I turned the car’s lights on and I could see that everything was working fine. Once the door was open again I could finish the job by wrapping the wire loom up with some cloth OEM look wire loom tape, but not on the resistor section as that may need to dissipate heat, not that it gets that hot anyway. The resistor section is insulated by the heat shrink and the rubber spade fitting covers.

Until I can get a good view in the dark and out in the open I wont be able to see if the light output is adequate or still too much. The results so seem to be what I’m after and not far away from the original bulb output, all be it a cleaner light.

With that in mind while the soldering iron was still hot and the resistors were out, I repeated the process for another inline with a resistance of 220 Ohms which will allow a little brighter light than the installed 330 Ohms. It will only take seconds to swap out which is the beauty of this idea. If the result still isn’t what I’m after, I can just knock up some more variations until I’m happy. There is no after picture of the rear loom as it’s all hidden away again, and nothing to see.

The only visible difference is the cool white light instead of the dull orange glow of the original incandescent bulb. The change to the lighting type of the cool white light picks out the silver lettering from the black background of the licence plate better for more effect.

Before & after comparison of the resistance hack:

A short and sweet little project from something that was in the back of my mind that needed addressing at some point. It’s funny how a chance conversation can lead to these little projects, all sorted for now.

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Don’t Be Negative

After last week’s post I had some great messages left for me and couple of nice emails too, so thank you. It was pointed out that I hadn’t actually posted a pic of the Krooklok in the car. Yep, I missed out one of the main points of what it looked like in the car. So to make amends here they are;

I don’t think it looks out of place either. Those with eagle eyes will spot that the pedal end of the lock is not shiny. Correct and this is something I eluded to in the last post. The metal end will damage paintwork on the pedal so i wrapped a little wire loom tape around it. This is a cloth tape and will cushion the metal on metal. On modern cars where the pedals are pretty much out of sight I wouldn’t need to do that. But as the Mustang pedals are clearly visible from outside the car chips in the black paint would look rather nasty. Also the cloth tape blends well to the pedals too.

While I was in the garage I had a little clean up under the hood, nothing special just a quick detailer wipe over to get some dust off. While I was at it I decided to change something that has been annoying me for quite a while now. This was the Negative battery cable terminal.

OK, so it doesn’t look wrong considering this isn’t the original wire, but a replacement cable for some reason or another. But, it looks sort of period correct so I left it, until now. I sourced a much more stock looking terminal and set about swapping them over.

The old terminal was a simple two screw squash the cable idea, simple enough to remove and will allow for corrosion for the exposed ends of the cable.

The cable separated easy enough and I cleaned it up with a wire brush to get it clean as possible. With the cable cleaned up I got my gas powered soldering iron out to prep the wire ends with some solder. As I was dealing with solder I put the heat resistant pad on the battery to stop any hot drips marking the plastic. The “Tinning” (a pre applied application of solder to aid in the final solder), had to be build up until a nice coating was all the way round the wire. I even cut back the sheath of the cable to expose some fresh wires. I slid a heat shrink tube over the cable which I would use later to give the finish a much cleaner look.

The next step I had to skip a little as I had one pair of hands to take the pics and do the work. I inserted the cable into the new terminal and clamped it in place with the two nuts on the top. Some stray long strands of wire were snipped of flush to the end of the terminal. With the cable in place I used some long nosed mole grips to hold the terminal up so I could fill the gap in the terminal with more solder.

This would give that neat finish I was after and make a great connection to the battery. My Dremel mini sanding discs were used flatten down the end as solder is a soft metal. With the end nice and flat the heat shrink was moved up to the terminal to cover any any gaps from the terminal and wire. Now the cable looks much nicer and neater and more importantly, the original stock look I was after.

I was able to refit the tightening bolt to the terminal and reconnect back to the battery.

The only remaining part now is to put the battery tag back on. I really am looking for things to do on the car now that don’t really need doing – just so I can do it. It only took about two hours from start to finish with the whole thing being cleaned and polished up. Well worth it as the wife was writing lots of lesson plans for her school. I was best out of the way! I think I may tidy up the other cable as well now. Also clean up the mats as they are pretty dirty too.

One of the simple little jobs was to swap out the interior bulbs for the LED equivalent. These included the footwell courtesy lights, and the rear centre console lights. They had the standard tungsten filament bulbs which gave out a warm glow. Not that I disliked it by any means, in fact that was the stock lock, I just wanted the more modern subtle look of a bright crisp white illumination.

The interior LED’s give out about three times as much light and shows of the internal colour scheme a bit better too. The pick above right was taken inside my garage and not outside in the sun.

What’s the next little job? I will think of something. 😉

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