Bearing Up

This year I have taken my car out for a couple of shows and I have developed a rather annoying squeak from the drivers side front wheel. I have taken the wheel of and greased everything that had a nipple on it. I squirted, white grease, silicon spray, Würth Water Dispersant, WD40 everywhere I could. Nothing. It was still there.

I spoke to Adam a couple of times about it and he advised me to bring it down and he would have a look at it. So I did just that.

The photo’s in this post I’m using have been given to me by Mustang Maniac and saved me taking the pictures; big thanks to Mustang Maniac for that. They told me they were probably going to use them this weekend. It looks like they beat me to it by posting first. So we have a little overlap although they have a couple of different pictures on their post.

Adam was walking to the yard and heard the squeak as I was turning into the yard’s driveway. I explained that I think the steering doesn’t feel right either. He listened intently and promptly jumped in my car and took it for a test drive up the road.

We swapped places for the driving seat as Adam need to swap a few cars around in order to get a clear run for my car onto the ramps in his workshop and I drove it in. Reinforcements arrived in the form of Yogi who had emerged from his workshop to help out with the diagnostics which is a two man job.

First thing they noticed was that the idler arm had some play. It looked like that over time standing in my garage the rubber had perished and broken down when the car came out for some shows this year.

You can see them when compared just how much the old one had broken down. The new one is on the left of each picture.

The guys checked everything else over on the suspension and I received my bollocking for a couple of other nuts that were loose. 🤦🏻‍♂️ Probably down to the play in the idler arm making things worse. Adam and Yogi both worked up and down under the car to check everything was tightened up as it should be. A couple of rear axle nuts were not as tight as they should be and Adam again tightened them up. I would like to say that in my self defence Adam does have a two foot long Snap On 1/2″ fitting breaker bar, to make sure things were properly tight.

They fitted the new idler arm and checked that the the locating bracket had no play with the arm fitted in place. Once they were happy I was sent out on another road test. Both Adam and Yogi told me that the steering would feel very different. The picture below is the new idler arm being fitted before full greasing.

I got out the main gate and and immediately the car felt different. I couldn’t believe just how bad it had gotten over a course of couple of years. You just get used to it and think no more of it.

I turned back into the yard happy, the squeak was still there, although not as bad now. Straight back onto the ramps and up in the air again. The guys decided that the wheel was to come off and have a look. They did all sorts of play checks and listened to the rotor spinning.

A decision was made fairly quickly. Yogi dropped the outer bearing out to check the look and feel of it. He wasn’t happy with it. Yogi then cleaned it up and Adam had a second look under the big lighted magnifying lens on his bench, nothing visibly wrong with it to look at. He stuck the bearing on his fingers and felt it, spinning it fast, slow and twisting it etc. Adam said “although it looks fine, I just don’t like how it feels, nope, I’m not happy with it”. With that he went of to the shop to go and get a new one.

In the mean time Yogi cleaned up the track of the bearing and made sure it wasn’t damaged by scoring or pitting. Luckily for me it was OK. The inner bearing was still fully packed. While we waited Yogi then proceeded to grease everything he could see, upper arms, lower arms, steering, bushes the lot.

Adam returned with the new bearing repeating his feel tests as he walked back to the ramps. “That’s better” he announced handing it over to Yogi. He repacked the new bearing with grease, rechecked it and fitted it back into the hub and adjusted it up correctly. He then replaced the retaining washer, split pin and the bearing cap. The wheel was put back on and retested for play and feel before letting the car back down.

I was then sent back out on the second test run to see how it was. I arrived back with a smile as big as my front grill. The noise had gone. Sorted 👍

Before I set off for my run I was told that if all was OK, to park out the front of the offices. Which I duly did as i was now well chuffed. They asked me if it was OK to use on the their blog posts. Of course I had not objections at all, they then took a number of pics of my car for their ‘Park & Pic’ section on their forth coming blog. Www.mustangmaniac.org

I love this picture as there is an early Falcon convertible, which of course was the Mustang’s immediate predecessor that shares the same chassis as First Gen Mustangs, and also a later Mustang all in one shot.

I sat in the offices with Adam and we had cup of tea, well he did and I had a cold can of pop. We put the world to rights, sorted out the bill before I left for home. The journey home was a pleasure until it started to rain. I was not impressed that my car had now gotten wet of course. But, considering the car was now in a another league, I wouldn’t mind.

I arrived home some hour and half later after filling with fuel (again). I just had to clean my car before I put her away and cover her up. I then plugged in the battery maintenance unit to keep the battery in tip top performance.

Again a huge thanks to Mustang Maniac (Adam & Yogi) for fitting me in and sending me home all on the same day. That is what I call “proper customer service.”

Before I sign off I just need to wish my friends on the other side of the pond;

Happy Independence Day.

Have a great day and have a beer for me. 🙂

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Before & After

I have had some emails saying why don’t I do a before and after photo set of the restoration? Then I got to thinking as to why I hadn’t up till now. There was no reason, so this post may be cheating a little as there is nothing new here. But what is new is the fact they have never been compared side by side before.  As I didn’t start my blog until a year after I bought the car, some of the earliest pictures don’t exist as such, during that time I had re-wired the car for the first time, managed to fire the car up, got the locks working (sort of), painted the trunk section and interior floor pans. Obviously if I had of known I would be doing a blog at that time, I would have documented it all much better than I have done. However my early work was re-done once the car had got to Mustang Maniac. Under their supervision and help it would be done “Properly” as Adam told me. So in effect you are indeed seeing the restoration from scratch, all be it not as bad as it was. I suspect that I would be playing catch up to keep on top of the car all the time to keep it looking good, especially with the original route I was going to take, ie; the amateur way.

Body Work:

 Rebuilt Back End:

Underside:

This was the old underseal, dirt and what ever else was squirted on there. Welded, ground down, filled, sanded down, painted with red oxide and painted with proper underseal and satin black paint.

Doors, Roof and Sides:

Rebuilt Front End:

Interior:

Inside was originally treated with POR15 for rust protection. This was later removed and proper sealant applied at paint and then primer and top coats. The last step was the Dynamat sound proofing, before the carpet that is.

Engine:

The story here was that I wanted to go sort of modern with the silicone look. As I knew I wanted a blue look to the car I went for the blue silicone and the blue spark plug leads. I went of the idea and eventually swapped them for the revised black and chrome look. The spark plug leads were changed at the last month as was the valve covers. The cable routing went through a number of variations until I was happy with it at that point. Rewire of the car was the first job as I had to see if the engine started, which it did on the second turn of the key after twelve years of standing years. Pretty impressive.

Transmission:

Steering and Suspension:

Brakes:

Even the brakes look as good as the outside of the car. The front drum brakes were replaced with disc brake conversion for stopping power and safety. The brake servo was original from the factory but was upgraded to dual system, again for safety.

Electrical:

All electrics have been replaced and the bulbs converted to LED where I can.

Glass and Bright Work Trim:

Paint Process:

There are hundreds of photos I could add here but I have kept it to the more key stages of the process.

Transportation:

These were some interesting shots of the car coming and going to different places.

Driving Her:

Special Thanks:

I have mentioned this before, but none of this would have been possible without the help and moral support from Mustang Maniac and their associates; Adam, Al (Yogi), Paul (Lob Monster), Chris (Careful), John, Paul (the paint), Lance (OCD from Marketing). I have learned so much from them all, above all I have gained some great friends who have all helped me realise a life’s ambition and dream come true.

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Water Works Problems

A day a Mustang Maniac is one of life’s pleasures, car talk, lots of cars and above all great company. Saturday the guys were sorting out the yard and moving stuff around again, the yard looks so much bigger now. The inevitable tea break allowed a relaxing few moments in the sun to listen what the plan was going to be for the day. The task was to finish up the electrics Once the neutral safety switch had been fitted. The fitting was two bolts slid over transmission selector lever. The twin pairs of wires were to be connected to the loom to stop the car turning over in anything other than Park or Neutral or the gear box. As the wire colours and fittings don’t match to the loom it was a case of using a Power Probe to manually switch on the back up lamps, and then make sure the car wouldn’t start in any gear. The initial educated guesstimate was correct and allowed the wires to be spliced in with proper tight fitting connections. The wire loom could now be sealed up to make it look stock. Adam was around to help out with Neutral Safety and as the battery was connected up a decision was made to check the headlights. Nothing, the neat cable work under the dash was pulled open and the relays were checked, nothing. The relays were removed and more Power Probe work was used to search out the live feeds. When manually triggered the headlights worked, that was a good sign at least. Adam asked if the fuses were OK, and of course took the statement “Yep, they are fine” as it was intended as a statement. Adam had a customer turn up to collect a large batch of body work and got “Lord” Yogi to come in and offer a look. Many shouts of “they on yet?” Resulted in a forlorn “Nope” response. This went on numerous times, and with lots bleeps later, still nothing. Then a consultation with the “book of words” reveled the problem. When the loom was fitted the “Live feed restricting connection and disabling function device”, ( I just made that bit up) or better know as a “Fuse”, was not in the fuse holder board. Yogi plugged in the correct rated fuse, the switch was turned and the lights came on, no problem. This explained the lack of a live feed. Needless to say “Lord” Yogi dished out some friendly abuse yours truly, all totally justified of course. When Adam asked what the problem was, no matter how much you try to disguise the fact that the “fuse” was missing by making up fancy words for it, a certain amount of banter often followed. Adam nailed the problem straight away earlier on, but choose to take the word of somebody who hadn’t checked their own work, it was a school boy error, OK. Everybody is allowed one now and again. Lol.

The latest delivery of Adam’s also included the custom fitting Monte Carlo stainless steel bolts that matched the export brace. The correct positioned holes were fitted and the bolts tightened up. The effect is pretty darn cool.

The next job was the wiper functionality and washer jets. The two-speed wiper motor was restored and looked pretty good. The down side was the two wires didn’t say what was the poss or the new side of the motor. So the plan is to put a pipe on the bottom of the pump and rest it in a jug of water and manually Power Probe it into operation. Yep, it made the correct noise, but made a complete meal out of and did nothing. The connections were swapped around and still nothing. Adam filed in his new storage area – the scrap bin. A sparkly new pump was sourced from the ever-expanding stores and the experiment was repeated. This time a gush of water duly sprouted forth as it should do. Two more holes had to be drilled into the inner fender panel to make it fit correctly.

waterjet3

The water bag was hung on the hooks and the rubber tubing fitted.

waterjet2

The pipe work was run around the loom location and run to the cowl. Washer jets were proudly displayed to Adam who looked at them and filed them under his new system “B” for Bin. Although they had cleaned up Ok the ends were flattened and wouldn’t have made a correct jet. So new ones were fitted. Two simple screws held the brutally simple pipe just under the cowl bars.

waterjet5

To finish up the day the loom was recovered with tape and neatened back up. Figuring all the issues out took up a fair bit of time. To complete the day the windows were cleaned up and the car has taken on a whole new look. Again not too much to look at this week as it was tidying up and correcting issues with the “Electrical restriction unit” or fuse.

Adam came around at the end of the day and decided to authenticate the restoration. He bought down one of the coveted Mustang Maniac labels. It simply has a number on it. Mine is 35, this is a badge of honour to say the work is worthy of the assigned number.

A great way to end the day – well chuffed.

resto35

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Bright Lights & Chrome

After a long week at work I didn’t think the weekend was ever going to get here. I had the car packed the night before to get to Mustang Maniac without any delays. Well that was apart from me dodging, rabbits, pheasants and any other form of livestock that decided that it wanted an early death by car! I managed to avoid all of them and my horn got used more time on that trip than the previous ten trips I reckon! Anyway I arrived to sea of people at the offices with Adam’s desk surrounded by customers at one point. I waited my turn to even say hello and discuss my plan of action. The plan was simple, rear bumper! This sounds like an easy task, but they can be a real pain if the bumpers are out of shape or don’t fit to the light panel. As the rear end of the car had been rebuilt this was going to be a moment of truth. I decided to take some pics of the process as I went along. I did get a helping hand from Yogi and Adam who popped in to see how I was doing. Apparently I was being a bit of wimp when it came to tightening the bolts up. The chrome bolts were sitting slightly proud and looked OK. The guys said that is not good enough and give it proper tightening up which pulled the bolts into the bumper and sat flush. The second side was a bit easier as I knew what to expect. I call it a learning process for me.

The whole set up comprises of a set of deluxe chrome bumper bolts, bumper irons (which I never had), mounting bolts and set of mounting pads to go between the bracket and the rear light panel.

The rear number plate fitting was screwed in first and only held in by two self tap screws. The wire will need to be long enough to get through the rear light panel to be connected to the rear side lights part of the loom.

Next up was the bumper irons, these will only fit one way and are shaped to the bumper itself with the angles.

The bolts are pushed through the squared out holes and the sprung washers are fitted over the bolts. Again these will only fit one way up due to the collar on the chrome bolts.

The bracket has to be massaged into place to fit the irons and to try to get the bolts to sit flat. This a bit of an art that I didn’t have before. Yogi loosened it all off and readjusted the positions and cranked on some pressure, this was to collapse the bumper washers to the irons forming a good fit, and to also pull the bolts down into the bumper itself. rbump11Both sides are exactly the same and there is no left or right hand sides on these parts. The mounting bolts are put through a large washer pushed out the light panel, a mounting pad made of dense foam goes over the bolts. The pads are tight around the bolt and will hold it in place to the light panel. The two-man job to align the bumper to the bolts goes without question, and the top bolts are tightened finger tight to hold the bumper in place. At this point Chris was extra set of eyes sitting further back behind the car to advise, “up a bit, down a bit, over a bit, wooo – too much” etc. This turned out to be a great help. We needed to move the bumper over a bit as it wasn’t exactly central so Yogi give it little nudge to adjust it up before the final tension on the bolts was done up. From underneath the bumper you can see the bolts into the irons. The two bolts each side are able to move inside the slots for the bolts to allow some movement to align them up. A trick of the trade was used to help align the bumper, but I have been sworn to secrecy on that one. I will say that it’s a great trick though.

rbump12

The down side is photo’s couldn’t really be taken as we were holding the bumper. The result was brilliant, a fantastic fitting bumper, as good as I have seen anywhere. Well chuffed with it.

rbump16

The rest of the day was involved in me completing the wiring at the back of the car and wrapping it with loom tape. As the LED light board had its own wires I soldered the connections in place to remove any opportunity for a poor connection. Heat shrink tubing was used to seal the soldered wires and then the full loom wrap. All of which you won’t see because it hidden out-of-the-way. Just a minor detail that nobody will see or notice except for the people who know, such as the MM guys who won’t let me get away with shoddy workmanship! Adam wanted to check out the rear loom was working fine and he used the Power Probe to make the LED boards in place.

Back up lamp.

backuplight

Side Lights.

sidelights

The indicator lights never seem to show up as amber very well on these pictures, but trust me they are bright.

indicators

The Brake lights are very bright too, so a huge upgrade to the standard Mustang lights.

brakelights

All in all a great day as a major part was fitted and it looked like I done something. Next week I’m not so sure what I am up too, but I have some more under hood tidying up to do. It’s all part of the adventure of bringing the car back to life. Waiting for next week already! That moment of truth of was talking about earlier on – no need to worry, it all fitted up without any major issues.

Thanks to the Guys, Adam, Yogi for the extra pair of hands and Chris for the extra pair of all-seeing eyes. 🙂

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Face Lift

A hot sunny day was promised for my weekend and I was looking forward to doing some work at Mustang Maniac. What we had planned was to fit the rear bumper, that meant that the car was loaded up with my big shiny bits that had been hanging on the wall for the last two years. I arrived all nice a cool as the Aircon had been on full whack all the way down there. You may have noticed that I am in a different workshop now. I have been promoted! I am now in Adam’s finishing workshop where there is more room to have the doors open and not worry about the sides.

finishingshop1

 

A conversation with Adam about the plan for the day changed slightly. We decided it was time to put the lights into the front of the car and tidy up the wire loom. Of course the wire loom work means that there is virtually no difference to look at except the people who know. I mentioned to Adam that the wire loom wasn’t long enough to go to the right hand side of the car for the lights. Adam looked at the routing I had done for the wires which was lovely and neat and tidy by the way, and said they were in the wrong place that’s why. Originally I had ran the light loom through the chassis under the radiator to keep it all neat and hidden. Trouble is that the depth to go down the lower front chassis and back up again behind the battery meant I  was about eight inches to short to meet up with the side or park lights. The main headlights would be fine as the wire was plenty long enough, so as I didn’t want to cut into the wires a re-route of the cable was the only option. I replaced the loom tape with the much nicer cloth loom tape to match the rest of the loom now, oh by the way – I seem to have shares in wire loom tape company now, the shares have shot up since I started on my car. With the routing in place where it originally should be the cables reached fine and I could actually cut them down a bit to the correct length.

Replacing the Head Lights

If you need to replace the parts like I did as most had gone to the great scrapyard in the sky then there are complete packs for the headlight assembly.

headlight21

The headlight bulbs are mounted behind the headlamp door which in turn exposes the retaining ring which is nice shiny bit of chrome, if you’re lucky. To replace the sealed beam is a fairly quick process, four screws on the headlight door and the three on the retaining ring. The bulb will fall forward and pull the loom plug off the back of the three spade connections. To refit, repeat the process in reverse. The bulbs I would be using are the H4 sealed unit bulbs to retain that stock look on the glass lens. There are modern alternatives that can be used in place but could require the bowl to be cut to allow them to be fitted correctly. As I have LED’s at the front so I will use them as daylight running too.

What I aim to do here is to show the complete headlight rebuild with the Scott Drake hardware kit. Attach the four new clips to the outside of the headlamp assembly making sure they are the correct way round with the threaded part to the back. Once these snap into place they can moved around by a couple of millimetres to enable the headlamp door to align to the fender correctly.

The next part is slightly more tricky as the adjustment studded threads have to be fitted. The retaining clips for the studs has a white washer/nut in the middle. These clips are pressed into the holes at the top and side for the adjustment. The legs on each side stop the fittings falling through the to the back of the buckets. With the legs on the front side the backing part of the fitting needs to be pressed behind the headlamp bucket assembly. If these are to tight bend the legs slightly forward to enable the fitting to sit further back into the hole and allow it to slip behind the back plate into place. There is a small amount of movement here to allow the bowl to fit.

There are two long threaded studs that have a recessed groove at the top. Screw the two studs into the nylon washer/nuts a few threads.

headlight6

Next it’s the headlight bowl itself, the only tricky part of this is the spring which I will explain in a couple of mins. Around the outside of the bowl there are two cut out lugs and a rectangle cut out. The lugs will locate in the collar of the studs. This will enable you to wind the stud either way to adjust the angles of the beam now.

The bowl is a loose fit at this point, so a spring is required to pull the tension against the studs and to stop the lens itself moving around. The spring is located into a hole at the back of the bucket and pulled through the bowl opening at the bottom to create the tension. Previously I had made one of the spring tools, but as I had left it at home it was the old school way of a fitting, a good ol’ pair of pliers. If you are going to use pliers, I would strongly recommend a long nosed pair of pliers with a very good grip. The spring itself is quite strong and needs a little bend just to get the hook of the spring over the edge of the bowl into the retaining eye.

With the bowl now in place you can add the bulb. Attach the loom connections to the back of the bulb and massage the wires into place at the back of the housing. (I couldn’t get pictures of this part as I didn’t want to drop the bulb).

Holding the bulb in place fit the chrome ring around the outside of the bulb lens and to the bowl, screw lightly into place on the bowl to stop the bulb falling out. Repeat with the other two screws.

The bulb is now in place and needs to be aligned up correctly. If the bulb is just a replacement then it should not need to be an adjusted. Adjust the beam with the studs to angle the lens on two axis points.

With the ring screws now in place, in future you should be able to unscrew each retaining screw a few turns so that the chrome ring will twist a little and lift over the head of the retaining screws.  This obviously makes it much easier for replacing the bulbs at a later date.

Once the bulb is aligned the last job is to refit the headlight door. Screw into place lightly and align the headlight doors back up with the with the fenders bevelled edges. That’s it – job done, quite simple.

headlight18

 

The wire loom took up most of the day and to route the cables nicely. The bulbs on the other hand didn’t take long and have given the car a complete facelift and now it looks like a mustang again, even without the grill. We connected the battery up and checked the park lights and they worked fine. The main headlights didn’t work yet as they needed to have an earth connection under the dash for the relays. But, it was exciting to see the car spring to life with the lights, almost as if she winked at me!

Thanks to Adam & Yogi who showed me the tips and tricks of the trade fitting the headlights.

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She’s Alive

What an epic day down at Mustang Maniac yesterday, I was so chuffed I can’t put it into words. OK, that’s not strictly true as I’m gonna tell you all about it. So I knew this weekend was going to be a day where it could be possible to start my car in theory. I was going try to start the wiring up again in order to turn her over on the key. Adam just looked at Yogi and laughed with “don’t worry about that, it will start!” Slightly confused, I sort of guessed what was going to happen when Yogi got out his little box of tricks and made up a lead while I fitted my Replica Autolite Group 24 Battery to the tray. They said that I would need some fuel for the car and I was packed off with an old school Jerry can and my wallet. I guess I had better get used to this filling the Muzzy up lark! I was given directions on how to get to the petrol station which was only a couple of miles away, it didn’t go in so I asked again, to which Yogi just laughed. So of I went, found it after over shooting the turning. Now I am not saying this place is old school, but there was a hut between two pumps and the sign said “Service fill only.” The bloke came out and got the diesel nozzle out, “No mate – fill this up unleaded” as I gave him the loaned Jerry can. With the can filled up and returned back to the yard, all without a SatNav. Yes, I admit it – I’m useless with directions, so much so that the very first thing my wife bought for me years ago when we got together was a TomTom. To which she said to me “Now I know you’re going get home,” Yep, she can have that one,  as I have genuinely got lost going home before now. Anyway, we got a funnel in the filler pipe of my car and poured some fuel in. We sloshed it around a bit by rocking the car and then lifted the car back up in the air and drained it out into a clear container to check the fuel. It was fine, clear with no debris in there. The fuel poured back into the tank. At the front of the car Yogi had now created his “Hot Wire” scenario and was ready to turn the car over. Now I could tell you how to start a car bypassing all the electrics on the car, but I won’t for obvious reasons, but it’s clever. Adam and I joined Yogi and he done his thing, the car turned over for a while until Adam and Yogi where happy there was no bad news noises on turn over. This was a very wise check to make sure the crank was not going to shatter or valves dropped on pistons etc. Adam now under the car turned the engine over by hand with a large ratchet to line up the TDC on the timing mark. Yogi then set the distributor shaft itself to where it should be, based on experience at this point of course. He then set up the wires to produce a spark and Adam pumped a little fuel in the carb and Adam now got to the front and was ready to adjust the timing on the distributor, Yogi spun the car over. The car turned over for a few seconds, she coughed and spluttered and fired up after a few seconds. The timing was adjusted by Adam and they wedged opened the butterfly on the choke to slow the engine down. She lives! The engine was shut down after a minute or so and a blur of hands worked over the engine to adjust things and tighten things up. Like watching synchronised swimming, but this was two guys saying only a few words and flurry of well rehearsed activity. The movement stopped, and the car turned over and she started up pretty instantly. This time the engine was getting quitter and was smooth, but that was the exact opposite of what was going on at the exhaust end. The burble and noise from those Flowmasters was fantastic as I now stood at the back listening to duet of exhaust notes and thunderous air vibration. The unique tone of my car was now heard for the first time, trying to take in the sounds played around my ears was incredible. The throttle was now starting to be pulsed by the guys, the exhaust note changing rapidly into a throaty bark. The timing light was now out and some very fine tuning was coming into play. Yogi was tweaking the carb and Adam was checking the fluid levels and making sure there were no leaks. The engine now slowed to an unmistakable throb of the 289 v8. Three blokes looked well chuffed as John and Chris popped over to see the action. The engine now stopped and quiet except for the ticking of the cooling engine filled the air, all I couldn’t say anything. I was ecstatic that the car fired up one step closer to driving her, and relief that my  and the guys hard work so far hadn’t gone to waste. The road test will need to be done obviously, but for now – I was a little gob smacked and overwhelmed with excitement a milestone had been reached. So far so good.

The fitting of the last part of the fuel line to the carb was the “banjo”, this turns the direction of the pipe ninety degrees  and an adjustable to the main fuel line. Yogi had set up the rubber hose ready for the fitting of the part. The filter from the carb was fitted into the end of the banjo.

The complete fitting was carefully lined up and tightened up to the carb, the angle of the pipe matched to the fuel hose. The hose was pushed on and tightened up.

Previously in the week the export brace had been fitted to the bulk head and the shock towers. Adam tells me that they used their custom-made conical fit bolts for the export brace, without having to file the holes square to make them fit. The bolts used are dome headed and stainless, not the nut and bolt of the original fitting and how they were then. These conical bolts fit into the standard holes and the tightening of the nut pulls the bolt into the brace tighter wedging them in so they don’t move. The result is pretty instant to look at and makes a big difference to the feel of the car. There is a common fault with fitting the export brace to a unstrengthened bulk head. The original export cars had a reinforced plate welded in place, this can be seen clearly on my car here too. The good news it that the brace fitted without need for cutting and adjusting to make it fit as some cars need. The reason is that those cars could have been in a little knock or “fender bender” and distorted the chassis. The work the guys had done on the jig was just perfect as always.

brace1

The guys left me to get on with the rest of the jobs under the hood, that was now to fit the wires to the oil sender, water temperature, electric choke and the ignition feeds to the coil, all can now be routed where I wanted them. But that was to be after a cup of tea, a few cakes and a bottle of chilled Dr Pepper. All these little jobs took longer than I thought they would, but who cares? My little lady is alive again and I still had that silly grin on my face. I have just got to say a big “Thanks” to Adam and Yogi for starting her up with me and showing me how to hot wire my car, just in case of emergencies of course. 😉

What an AMAZING day, thanks Mustang Maniac.  

My car may well be at the Enfield Pageant of Motoring this coming weekend with Mustang Maniac’s other cars. It’s a great show so wander over and have a chat with guys. The details can be found at this link:

http://www.whitewebbsmuseum.co.uk/html/body_enfield_pageant.html